FSDM0365RL_NL Fairchild Semiconductor, FSDM0365RL_NL Datasheet - Page 11

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FSDM0365RL_NL

Manufacturer Part Number
FSDM0365RL_NL
Description
Manufacturer
Fairchild Semiconductor
Datasheet

Specifications of FSDM0365RL_NL

Power Switch Family
FSDM0365
Power Switch On Resistance
3.6Ohm
Output Current
1.89A
Number Of Outputs
Single
Mounting
Surface Mount
Supply Current
3mA
Package Type
LSOP
Operating Temperature (min)
-25C
Operating Temperature (max)
85C
Operating Temperature Classification
Commercial
Pin Count
8
Power Dissipation
1.56W
Lead Free Status / Rohs Status
Compliant
5. Soft Start : The FPS has an internal soft start circuit that
slowly increases the feedback voltage together with the
Sense FET current after it starts up. The typical soft start
time is 15msec, as shown in Figure 8, where progressive
increments of the Sense FET current are allowed during the
start-up phase. The pulse width to the power switching
device is progressively increased to establish the correct
working conditions for transformers, inductors, and capaci-
tors. The voltage on the output capacitors is progressively
increased with the intention of smoothly establishing the
required output voltage. It also helps to prevent transformer
saturation and reduce the stress on the secondary diode.
6. Burst Operation : In order to minimize power dissipation
in standby mode, the FPS enters burst mode operation. As
the load decreases, the feedback voltage decreases. As
shown in Figure 9, the device automatically enters burst
mode
V
limit is set to a fixed limit internally to minimize flux density
in the transformer. The fixed current limit is larger than that
defined by V
down further. Switching continues until the feedback voltage
drops below V
and the output voltages start to drop at a rate dependent on
the standby current load. This causes the feedback voltage to
rise. Once it passes V
The feedback voltage then falls and the process repeats.
Burst mode operation alternately enables and disables
switching of the power Sense FET thereby reducing switch-
ing loss in Standby mode.
2.15A
0.98A
BURH
Drain current
(500mV). Switching still continues but the current
when
1ms
Figure 8. Soft Start Function
FB
BURL
the
= V
(350mV). At this point switching stops
15steps
BURH
feedback
BURH
Current limit
and therefore, V
(500mV), switching resumes.
voltage
drops
FB
is driven
below
t
7. Frequency Modulation : Modulating the switching fre-
quency of a switched power supply can reduce EMI. Fre-
quency modulation can reduce EMI by spreading the energy
over a wider frequency range than the bandwidth measured
by the EMI test equipment. The amount of EMI reduction is
directly related to the depth of the reference frequency. As
can be seen in Figure 10, the frequency changes from 65KHz
to 69KHz in 4ms for the FSDM0365RN (48.5KHz to
51.5KHz for FSDL0365RN). Frequency modulation allows
the use of a cost effective inductor instead of an AC input
mode choke to satisfy the requirements of world wide EMI
limits.
Vfb
69kHz
67kHz
65kHz
Waveform
V
V
Current
3
BURH
BURL
Figure 10. Frequency Modulation Waveform
f
s
=1/t
V
V
I
FB
BURL
DELAY
s
Figure 9. Burst Operation Function
V
Vcc
BURH
/V
BURH
Operation
t
Burst
Vcc
s
+
-
I
FB
Current
Switching
Drain
OFF
2.5R
4ms
R
Normal
Operation
Burst
FSDL0365RN, FSDM0365RN
Burst
Switching
OFF
Vcc
I
BUR(pk)
Operation
Normal
MOSFET
Current
PWM
t
11

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