LTC3615 LINER [Linear Technology], LTC3615 Datasheet - Page 20

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LTC3615

Manufacturer Part Number
LTC3615
Description
Dual 4MHz, 3A Synchronous Step-Down DC/DC Converter
Manufacturer
LINER [Linear Technology]
Datasheet

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Figure 5. Load Step Transient in FCM with External Compensation
LTC3615
applicaTions inForMaTion
Applications section uses faster compensation to improve
load step response.
A second, more severe transient is caused by switching
in loads with large (>1µF) supply bypass capacitors. The
discharged bypass capacitors are effectively put in parallel
with C
alter its delivery of current quickly enough to prevent this
sudden step change in output voltage if the load switch
resistance is low and it is driven quickly. More output
capacitance may be required depending on the duty cycle
and load step requirements.
If the ITH pin is tied to SV
(AVP) mode and the internal compensation is selected.
In AVP mode, the load regulation performance is inten-
tionally reduced, setting the output voltage at a point that
is dependent on the load current. When the load current
suddenly increases, the output voltage starts from a level
slightly higher than nominal so the output voltage can
droop more and stay within the specified voltage range.
0
OUT
200mV/DIV
, causing a rapid drop in V
1A/DIV
100mA
V
3A
OUT
I
L
V
I
V
COMPENSATION AND OUTPUT CAPACITOR
VALUES OF FIGURE 3
LOAD
OUT
MODE
= 1.8V
= 100mA TO 3A
= 1.5V
IN
, the active voltage positioning
50µs/DIV
OUT
. No regulator can
3615 F05
When the load current suddenly decreases, the output
voltage starts at a level lower than nominal so the output
voltage can have more overshoot and stay within the
specified voltage range. This behavior is demonstrated
in Figure 6.
The benefit is a lower peak-to-peak output voltage devia-
tion for a given load step without having to increase the
output filter capacitance. Alternatively, the output voltage
filter capacitance can be reduced while maintaining the
same peak-to-peak transient response. For this operation
mode, the loop gain is reduced and no external compensa-
tion is required.
Programmable Switch Pin Slew Rate
As switching frequencies rise, it is desirable to minimize the
transition time required when switching to minimize power
losses and blanking time for the switch to settle. However,
fast slewing of the switch node results in relatively high
external radiated EMI and high on-chip supply transients,
which can cause problems for some applications.
Figure 6. Load Step Transient in FCM in AVP Mode
100mV/DIV
1A/DIV
V
OUT
I
L
V
I
V
V
OUTPUT CAPACITOR VALUE FIGURE 3
LOAD
OUT
MODE
IN
= V
= 1.8V
= 100mA TO 3A
ITH
= 1.5V
= 3.3V
50µs/DIV
3615 F06
3615f

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